State Senator Leland Yee And A Notorious Russian Arms Dealer

I’m in deep shock over the senator Leland Yee scandal. It goes far beyond a normal political corruption case. It sounds more like that Russian arms dealer Victor Blount who is now doing 25 years in a US prison. This man was plotting to sell all sorts of advanced weapons to terrorists. The same can be said for Yee. If convicted he’s guaranteed to get 25 years in prison. That will be a life sentence for him. If he still has his Chinese passport…well use your imagination.

Some Thoughts On One’s Death

One’s own death is not a pleasant subject to think about. I always tell Elena that the best way to die is to make beautiful love with someone that you care deeply for. Then you fall into a peaceful sleep where you never awaken again. Elena does not agree with me on this point.
Yesterday I was watching the new Cosmos series. They were talking about the famous British mathematician and astronomer from the 1600’s Edmond Halley. Halley’s comet is named after him. In his final moments of life, he drank a large glass of red wine. He then fell off into eternal sleep. Now that’s another great way to leave this life!

Each Day Of Life Is A Wonderful Gift

Elena got the sad news that a dear doctor friend in Argentina is sick with leukemia. As one gets older sad news like this comes more often. Each day is a gift and every morning that we get up, especially if we are healthy, is really special!!!!
When I was a young man growing up in Houston I was friends with a lady named Betty Gluckman. Her mother and father had both been inmates at the notorious Auschwitz death camp. They were both humble and modest people. They never had any hate in their heart for the Nazis. They never felt that life had been unfair to them. They never suffered from what we now called post traumatic stress disorder. To them each day of life was a wonderful gift to be treasured. We can all learn something from the Gluckman’s wonderful story.

An Electrical Fire Brought Down The Malaysian Airliner as per Chris Goodfellow

A Startlingly Simple Theory About the Missing Malaysia Airlines Jet
BY CHRIS GOODFELLOW03.18.146:30 AM
Image: Pedro Moura Pinheiro/Flickr
Image: Pedro Moura Pinheiro/Flickr
There has been a lot of speculation about Malaysia Airlines Flight 370. Terrorism, hijacking, meteors. I cannot believe the analysis on CNN; it’s almost disturbing. I tend to look for a simpler explanation, and I find it with the 13,000-foot runway at Pulau Langkawi.

We know the story of MH370: A loaded Boeing 777 departs at midnight from Kuala Lampur, headed to Beijing. A hot night. A heavy aircraft. About an hour out, across the gulf toward Vietnam, the plane goes dark, meaning the transponder and secondary radar tracking go off. Two days later we hear reports that Malaysian military radar (which is a primary radar, meaning the plane is tracked by reflection rather than by transponder interrogation response) has tracked the plane on a southwesterly course back across the Malay Peninsula into the Strait of Malacca.

READ MORE:
How the Missing Malaysia Airlines Jet Could Have Been Hijacked
Inside the Nearly Impossible Task of Finding an Airplane in the Ocean
How It’s Possible to Lose an Airplane in 2014
The left turn is the key here. Zaharie Ahmad Shah1 was a very experienced senior captain with 18,000 hours of flight time. We old pilots were drilled to know what is the closest airport of safe harbor while in cruise. Airports behind us, airports abeam us, and airports ahead of us. They’re always in our head. Always. If something happens, you don’t want to be thinking about what are you going to do–you already know what you are going to do. When I saw that left turn with a direct heading, I instinctively knew he was heading for an airport. He was taking a direct route to Palau Langkawi, a 13,000-foot airstrip with an approach over water and no obstacles. The captain did not turn back to Kuala Lampur because he knew he had 8,000-foot ridges to cross. He knew the terrain was friendlier toward Langkawi, which also was closer.

Take a look at this airport on Google Earth. The pilot did all the right things. He was confronted by some major event onboard that made him make an immediate turn to the closest, safest airport.

The loss of transponders and communications makes perfect sense in a fire.
When I heard this I immediately brought up Google Earth and searched for airports in proximity to the track toward the southwest.

For me, the loss of transponders and communications makes perfect sense in a fire. And there most likely was an electrical fire. In the case of a fire, the first response is to pull the main busses and restore circuits one by one until you have isolated the bad one. If they pulled the busses, the plane would go silent. It probably was a serious event and the flight crew was occupied with controlling the plane and trying to fight the fire. Aviate, navigate, and lastly, communicate is the mantra in such situations.

There are two types of fires. An electrical fire might not be as fast and furious, and there may or may not be incapacitating smoke. However there is the possibility, given the timeline, that there was an overheat on one of the front landing gear tires, it blew on takeoff and started slowly burning. Yes, this happens with underinflated tires. Remember: Heavy plane, hot night, sea level, long-run takeoff. There was a well known accident in Nigeria of a DC8 that had a landing gear fire on takeoff. Once going, a tire fire would produce horrific, incapacitating smoke. Yes, pilots have access to oxygen masks, but this is a no-no with fire. Most have access to a smoke hood with a filter, but this will last only a few minutes depending on the smoke level. (I used to carry one in my flight bag, and I still carry one in my briefcase when I fly.)

What I think happened is the flight crew was overcome by smoke and the plane continued on the heading, probably on George (autopilot), until it ran out of fuel or the fire destroyed the control surfaces and it crashed. You will find it along that route–looking elsewhere is pointless.

lang-660

Ongoing speculation of a hijacking and/or murder-suicide and that there was a flight engineer on board does not sway me in favor of foul play until I am presented with evidence of foul play.

We know there was a last voice transmission that, from a pilot’s point of view, was entirely normal. “Good night” is customary on a hand-off to a new air traffic control. The “good night” also strongly indicates to me that all was OK on the flight deck. Remember, there are many ways a pilot can communicate distress. A hijack code or even transponder code off by one digit would alert ATC that something was wrong. Every good pilot knows keying an SOS over the mike always is an option. Even three short clicks would raise an alert. So I conclude that at the point of voice transmission all was perceived as well on the flight deck by the pilots.

But things could have been in the process of going wrong, unknown to the pilots.

Evidently the ACARS went inoperative some time before. Disabling the ACARS is not easy, as pointed out. This leads me to believe more in an electrical problem or an electrical fire than a manual shutdown. I suggest the pilots probably were not aware ACARS was not transmitting.

As for the reports of altitude fluctuations, given that this was not transponder-generated data but primary radar at maybe 200 miles, the azimuth readings can be affected by a lot of atmospherics and I would not have high confidence in this being totally reliable. But let’s accept for a minute that the pilot may have ascended to 45,000 feet in a last-ditch effort to quell a fire by seeking the lowest level of oxygen. That is an acceptable scenario. At 45,000 feet, it would be tough to keep this aircraft stable, as the flight envelope is very narrow and loss of control in a stall is entirely possible. The aircraft is at the top of its operational ceiling. The reported rapid rates of descent could have been generated by a stall, followed by a recovery at 25,000 feet. The pilot may even have been diving to extinguish flames.

But going to 45,000 feet in a hijack scenario doesn’t make any good sense to me.

Regarding the additional flying time: On departing Kuala Lampur, Flight 370 would have had fuel for Beijing and an alternate destination, probably Shanghai, plus 45 minutes–say, 8 hours. Maybe more. He burned 20-25 percent in the first hour with takeoff and the climb to cruise. So when the turn was made toward Langkawi, he would have had six hours or more hours worth of fuel. This correlates nicely with the Inmarsat data pings being received until fuel exhaustion.

Fire in an aircraft demands one thing: Get the machine on the ground as soon as possible.
The now known continued flight until time to fuel exhaustion only confirms to me that the crew was incapacitated and the flight continued on deep into the south Indian ocean.

There is no point speculating further until more evidence surfaces, but in the meantime it serves no purpose to malign pilots who well may have been in a struggle to save this aircraft from a fire or other serious mechanical issue. Capt. Zaharie Ahmad Shah was a hero struggling with an impossible situation trying to get that plane to Langkawi. There is no doubt in my mind. That’s the reason for the turn and direct route. A hijacking would not have made that deliberate left turn with a direct heading for Langkawi. It probably would have weaved around a bit until the hijackers decided where they were taking it.

Surprisingly, none of the reporters, officials, or other pilots interviewed have looked at this from the pilot’s viewpoint: If something went wrong, where would he go? Thanks to Google Earth I spotted Langkawi in about 30 seconds, zoomed in and saw how long the runway was and I just instinctively knew this pilot knew this airport. He had probably flown there many times.

Fire in an aircraft demands one thing: Get the machine on the ground as soon as possible. There are two well-remembered experiences in my memory. The AirCanada DC9 which landed, I believe, in Columbus, Ohio in the 1980s. That pilot delayed descent and bypassed several airports. He didn’t instinctively know the closest airports. He got it on the ground eventually, but lost 30-odd souls. The 1998 crash of Swissair DC-10 off Nova Scotia was another example of heroic pilots. They were 15 minutes out of Halifax but the fire overcame them and they had to ditch in the ocean. They simply ran out of time. That fire incidentally started when the aircraft was about an hour out of Kennedy. Guess what? The transponders and communications were shut off as they pulled the busses.

Get on Google Earth and type in Pulau Langkawi and then look at it in relation to the radar track heading. Two plus two equals four. For me, that is the simple explanation why it turned and headed in that direction. Smart pilot. He just didn’t have the time.

Chris Goodfellow has 20 years experience as a Canadian Class-1 instrumented-rated pilot for multi-engine planes. His theory on what happened to MH370 first appeared on Google+. We’ve copyedited it with his permission.

The Missing Malaysian Airlines Flight Climbed To 45,000 Feet

I began flying on jet planes in June of 1967. My first flight was on a Boeing 707 going from Houston to Los Angeles. I was on my way to US Navy boot camp. I told my mother and father that it was thrilling to be able to urinate while flying at 35,000 feet.
In all of my almost 47 years of flying I must have flown some several million miles in the air allover the world. There was only one time that I thought that I was going to die on a plane. It was on a flight between Sao Paulo and Buenos Aires in February of 1980. The plane encountered such violent turbulence that I honestly believed that it was going to have a structural failure and break apart in the air. My palms were still sweating after we landed in Buenos Aires.
In my flying career I have flown as fast as 700 miles per hour. I have been as high as 42,000 feet.
Last night Elena shared with me some news about the missing Malaysian airliner. There is now an indication that it climbed to 45,000 feet. Elena told me that the goal of that climb was to render all of the passengers unconscious. She asked me if the pilots had oxygen masks. I assured her they did.
Elena believed that whoever was controlling the plane depressurized the cabin. She thought that it was to make the passengers pass out. I am sure that it was to kill all of the passengers. Hopefully the passengers fell off to sleep and never knew they were dying.
Statistically flying is safer than driving down the freeway. But some people in the air get very unlucky. This appears to be the case with the passengers on that flight.

Thinking Outside The Box Works!!!!

I did some original thinking yesterday afternoon that solved a long-running problem. My garage door opening system often fails. I have even had the wonderful people from A and H Access Control out to look at it. The diagnosis is that the sensors are super sensitive. They must be kept clean and free of debris. I have spent a lot of time cleaning the sensors. I have a lot of problems with getting the garage door to close. I had an inspiration yesterday afternoon. I have a blowing machine for clearing away leaves and vegetation from the drive way and sidewalk. I plugged it in and used it to blow all debris away from the garage door sensors. Now my garage door works perfectly!

The Monuments Men

Last night Elena and I saw a show called the Rape of Europa. It was about all of the art work at risk in World War II as the Nazis attacked and the valiant efforts by museum staff in Paris and St. Petersburg to save the art. It then spent a lot of time talking about the incredible work of a special US Army group with the nickname of “The Monuments Men.” (There is also a movie by that name playing now.) It was a spell binding story. The question that kept popping up in my mind was:
“Why has it taken almost 70 years to honor all of these brave people for their incredible work?”